Hi folks i'am new here I drive a one ton dually but fuel prices down sized me. I have a 1996 olds cutlass with a 3.4 engine and a 4t60 e trans. runs and drives great it just doesn't go into overdrive. any ideas? The SES light is on with a 1870 code
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is it not going into overdrive (4th gear), or TCC lockup? If it's the latter, it's usually caused by a bad Pulsewidth modulated solenoid. If you go ahead and disconnect it, it may start working again. Let me know and I'll find some data to help you.Brian
'95 Cutlass Supreme- "The Rig"
3400 SFI V6, 4T60e
Comp Cam grind, LS6 valve springs, OBD2 swap, Tuned
2.5" DP/ 2.5" dual exh/ Magnaflow Cat/ crap mufflers/ 3500 Intake manifold/ 65mm TB
TGP steering Rack/ 34mm Sway Bar/Vert STB/ KYB GR2's
'08 Chevy Trailblazer SWB 1LT "Smart Package"- LH6 5.3L V8/4L60e, A4WD
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It's a black wire, I believe Pin E on the transmission connector (under the engine airbox) This site has a diagram showing this but I can't seem to find it. It sounds like it isn't your problem though, but maybe it's worth a shot. If you just pop the pin out of the connector, and it doesn't change anything, just slide it back in.Brian
'95 Cutlass Supreme- "The Rig"
3400 SFI V6, 4T60e
Comp Cam grind, LS6 valve springs, OBD2 swap, Tuned
2.5" DP/ 2.5" dual exh/ Magnaflow Cat/ crap mufflers/ 3500 Intake manifold/ 65mm TB
TGP steering Rack/ 34mm Sway Bar/Vert STB/ KYB GR2's
'08 Chevy Trailblazer SWB 1LT "Smart Package"- LH6 5.3L V8/4L60e, A4WD
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Brian
'95 Cutlass Supreme- "The Rig"
3400 SFI V6, 4T60e
Comp Cam grind, LS6 valve springs, OBD2 swap, Tuned
2.5" DP/ 2.5" dual exh/ Magnaflow Cat/ crap mufflers/ 3500 Intake manifold/ 65mm TB
TGP steering Rack/ 34mm Sway Bar/Vert STB/ KYB GR2's
'08 Chevy Trailblazer SWB 1LT "Smart Package"- LH6 5.3L V8/4L60e, A4WD
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Just got back from a roadtrip to Minneapolis. On the way back I had a similar issue pop up and the transmission wouldn't go into full lock at cruise speeds. Turned out I was just low on fluid after one of my BRAND NEW fluid cooler lines (OEM-style) decided to leak. Thankfully it was just a slow leak and all I needed was 2L over a few stops to get everything working right again. Not sure what to do with the other 6L I bought incase it wasn't a slow leak.1995 Grand Am SE
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Save them for your next scheduled filter change :P-60v6's 2nd Jon M.
91 Black Lumina Z34-5 speed
92 Black Lumina Z34 5 speed (getting there, slowly... follow the progress here)
94 Red Ford Ranger 2WD-5 speed
Originally posted by Jay LenoTires are cheap clutches...
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common issue...
74k miles on that one, and ready to strip with a little more power... needless to say I replaced it when I rebuilt the trans.
Got Lope?
3500 Build, Comp XFI Cam 218/230 .050 dur .570/.568 lift 113LSA
Fully Balanced, Ported, 3 Angle Valve Job, 65mm TCE TB, S&S Headers.
Stage-1 Raybestos/Alto 4t60e-HD, EP LSD, 3.69FDR
12.61@105 Epping NH Oct 2015 Nitrous 100shot (melted plugs) 13.58@98.8 N/A 3200LBS
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did the fluid have a orangish tint to it when drained? if so bad torque converter... I have a E with that problem and just spent 1250 instead and got a E rebuilt.. didnt want to take out the converter to replace and later down the road have more problems..Robert
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96 Grand Prix SE 3100 202,000 miles
New Rebuilt 3100
New Rebuilt 4T60-E
Exhaust
Drilled/Slotted Rotors
95 Grand Prix GTP 177,000 miles
White
3" Magnaflow Catback
Lowered 2" Eibach in front Brichmount Rear
94-96 Hi-Po 5 Stars on 245/50/16
90 Pontiac Turbo Grand Prix
5 Speed Swapped
127,000
Spec Stage 3 Clutch
230,000 mile Getrag 282
Emissions Deleted
Brand new Engine 1,000 Miles
Fully Custom Built car
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Looks like I'm still having OD problems. This morning the car struggled to get into overdrive and keep it. On the way back from work though it was working as it always had so I'm a little confused. Fluid is still full and hasn't leaked so all I can think is either a sticky TCC solenoid or there was some more air waiting to bleed out of the system.1995 Grand Am SE
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If it comes and goes then your in good luck still. Check or change out the gear selector switch on the trans. One way to test to see if its out of range is to shift it into OD and go up to 50mph. Then ever so slighly try to move it up or down without shifting it into Nutral or Drive. DID you run a scan of the car?88 Beretta GTU turbo . 90 Black ASC/McLaren TGP, awaiting 4t80. 2003 Grand AM se 3400/4t45 daily grind.
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