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Any updates on this? track times/dyno #'s? Is it still running a stock cam?
I am thinking of doing a similar project to this my self but in a larger truck!
1999 Olds Alero 2.4 to 3500 swap (running). totaled by a honda
1992 lumina 4 door 3500 3spd auto 15.020 @93.5 mph
1984 Cavalier type 10 hatch 3100 5spd!!!
14.96@91.47 in the 1/4
9.63@74.36 in the 1/8th
14.30 on slicks! scrapped due to rust!
The truck was sold about two weeks ago. Supercharger was removed because belt would not stop slipping and was choking the motor at higher rpms. What it really needed to work was a dedicated crank pulley and belt, preferably 8-rib since the charger already had an 8-rib pulley anyway.
However the motor itself ended up being awesome; never burned or leaked any oil, plenty of power for a little truck like that.
I don't think a smaller pulley would have helped. It was choking the motor because the belt was slipping, causing the charger to turn too slowly. With the stock pulleys it was only making 4psi when the belt would start squealing at around 3000 rpm or so.
The belt was tight and wrapped 90% of the SC pulley. Crank pulley was wrapped less probably around 30-40%. I think the fix would have been a separate belt for the SC. Sorta like what the 3800s and T-bird super coupes have.
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